Search alternatives:
larger decrease » marked decrease (Expand Search)
we decrease » _ decrease (Expand Search), nn decrease (Expand Search), teer decrease (Expand Search)
a decrease » _ decrease (Expand Search), _ decreased (Expand Search), _ decreases (Expand Search)
larger decrease » marked decrease (Expand Search)
we decrease » _ decrease (Expand Search), nn decrease (Expand Search), teer decrease (Expand Search)
a decrease » _ decrease (Expand Search), _ decreased (Expand Search), _ decreases (Expand Search)
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4441
Type of Mutations.
Published 2025“…The docking research indicated that these mutations decreased the binding affinity for DNA, with R273C, R280G, G266E, and G105C displaying the most significant differences. …”
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4442
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4443
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4444
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4445
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4446
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4447
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4448
Impact of sludge dosage on HPST.
Published 2025“…The model optimization and experimental validation showed that the optimal HPST conditions for treating domestic sewage were as follows: the dosage of polyaluminum chloride (PAC) was 1.70 g/L, cationic polyacrylamide (CPAM) dosage was 2.35 mg/L, sewage pH was maintained at 8.0, sludge dosage was 10 mL/L, stirring time lasted for 5 minutes, and settling time lasted for 30 minutes. As a result of these optimized conditions, the turbidity of treated sewage decreased to 1.19 NTU.…”
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4449
Impact of settling time on HPST.
Published 2025“…The model optimization and experimental validation showed that the optimal HPST conditions for treating domestic sewage were as follows: the dosage of polyaluminum chloride (PAC) was 1.70 g/L, cationic polyacrylamide (CPAM) dosage was 2.35 mg/L, sewage pH was maintained at 8.0, sludge dosage was 10 mL/L, stirring time lasted for 5 minutes, and settling time lasted for 30 minutes. As a result of these optimized conditions, the turbidity of treated sewage decreased to 1.19 NTU.…”
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4450
ANOVAs for the response surface of Eq (2).
Published 2025“…The model optimization and experimental validation showed that the optimal HPST conditions for treating domestic sewage were as follows: the dosage of polyaluminum chloride (PAC) was 1.70 g/L, cationic polyacrylamide (CPAM) dosage was 2.35 mg/L, sewage pH was maintained at 8.0, sludge dosage was 10 mL/L, stirring time lasted for 5 minutes, and settling time lasted for 30 minutes. As a result of these optimized conditions, the turbidity of treated sewage decreased to 1.19 NTU.…”
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4451
Impact of CPAM dosage on HPST.
Published 2025“…The model optimization and experimental validation showed that the optimal HPST conditions for treating domestic sewage were as follows: the dosage of polyaluminum chloride (PAC) was 1.70 g/L, cationic polyacrylamide (CPAM) dosage was 2.35 mg/L, sewage pH was maintained at 8.0, sludge dosage was 10 mL/L, stirring time lasted for 5 minutes, and settling time lasted for 30 minutes. As a result of these optimized conditions, the turbidity of treated sewage decreased to 1.19 NTU.…”
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4452
Impact of sewage pH on HPST.
Published 2025“…The model optimization and experimental validation showed that the optimal HPST conditions for treating domestic sewage were as follows: the dosage of polyaluminum chloride (PAC) was 1.70 g/L, cationic polyacrylamide (CPAM) dosage was 2.35 mg/L, sewage pH was maintained at 8.0, sludge dosage was 10 mL/L, stirring time lasted for 5 minutes, and settling time lasted for 30 minutes. As a result of these optimized conditions, the turbidity of treated sewage decreased to 1.19 NTU.…”
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4453
Impact of PAC dosage on HPST.
Published 2025“…The model optimization and experimental validation showed that the optimal HPST conditions for treating domestic sewage were as follows: the dosage of polyaluminum chloride (PAC) was 1.70 g/L, cationic polyacrylamide (CPAM) dosage was 2.35 mg/L, sewage pH was maintained at 8.0, sludge dosage was 10 mL/L, stirring time lasted for 5 minutes, and settling time lasted for 30 minutes. As a result of these optimized conditions, the turbidity of treated sewage decreased to 1.19 NTU.…”
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4454
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4455
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4456
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4457
Schematic diagram of numerical simulation model.
Published 2025“…<div><p>After prolonged waterflooding development, the main integrated oil reservoirs in the X Oilfield have largely entered the late stage of waterflooding, with an average water cut reaching approximately 98%. However, a significant amount of remaining oil still accumulates in the weak water-flushed zones of low-permeability layers, which presents substantial development potential. …”
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4458
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4459
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4460